I flipped the switch on the Quad rotor to go into altitude hold with simple mode on. It then promptly freaked out did a back flip and thew it's self into a wall and dug its self into the drywall. any thoughts? Thanks....
P.S.- for some reason I have no Logs of it... any idea why?
I think so
When I have a violent unexplained problem I try to re-load code using the Arduino 22, resetting all values and recalibrate. You left little info on your setup, but it is always possible that after an upgrade that bad values are left in Eeprom. All my problems like this are resolved in this way.
Next time try it on soft grass. :}
maybe.. I have $50 in parts to get to try - try again.....