APM .6 in a Walkera X350 Frame - Won't take off.

Hello guys,

I know I have seen numerous posts on this topic, but I haven't really seen a solution yet.

After a crash, I rebuilt my Walkera X350 with the APM 2.6 Flight Controller with full telemetry.

Two days ago I flew my quad with the APM fitted and it was perfect.  Then I came home and fitted the GoPro and Gymbal.  Got that working, I also adjust the rate of descent for the quad.

BUT... it won't leave the ground now!!

I have tried everything from re-installing the firmware, making sure the batteries are charged, recalibrating the radio, making sure everything is OK.

I think the motors aren't spinning fast enough or the power to them is too little.

Is there anyway of increasing the speed and power of the motors?  I have made sure that Thr Max is right up, but still nothing.

Sensible answers greatly appreciated.

Many thanks

Malc

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Replies

  • Hey guys,

    Surely someone out there must know the solution?

    What I have done is restored all the defaults under the Full Parameter list, but as I am now out of the country, I've not been able to try it yet.

    So has anyone else seen this issue with other multis and what did you do to fix it?

    Thanks in anticipation.

    Malc

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