This is my first use of any type of autopilot so I am probably making some kind of rookie mistake. What my problem is that I put multi switch into stabilize mode the pitch response to airframe movement is backwards. I have been trying different ways to configure it on the radio setup page and can only get the problem to switch to a backwards roll response. Manual mode is fine and the stabilize setting responds to my rc input properly. Any help would be greatly appreciated. I know I am green and the problem is something simple , but we all gotta start somewhere right.
Switched servo to APM2 wires and all is good with my world.
What motor, prop and battery are you using, how fast are you flying, and how much time are you getting on your battery? Do you know your cruise amps?
I have only flown it once so far. Eflight 46 motor,2 x 4 cel 3200 battery in parallel, 15x8 apc prop, eflight 60 amp speed control. I have a 20 min flight video but I will have to get back to ya on the current draw next time I fly it. I cut the flight short because I lost my canopy or foam lid, whatever ya want to call it.