Anyone who can help me out the problem that my APM 2.0 board sensor output signal like unstable or noise ?
I take the video of this phenomenon.
Tags:
Permalink Reply by Whooper on January 19, 2013 at 3:55am Did you manage to fix this problem? I am having a similar issue. When the board is stationary on the bench (no GPS lock) the roll /pitch sensor output is stable. As soon as GPS gets a lock the pitch/roll sensor output becomes unstable and does not settle down to a steady value.
Season Two of the Trust Time Trial (T3) Contest has now begun. The fourth round is an accuracy round for multicopters, which requires contestants to fly a cube. The deadline is April 14th.184 members
1290 members
51 members
11 members
182 members
© 2013 Created by Chris Anderson.
Powered by
