Hi all. I'm glad to be on this forum, maybe my information will be useful.Today I did the mission flight, it was not my first flight, and everything was ok before.I've added 2 points: first at…Continue
I'm not asking about software tuning, but about such trivial things as protection case/normal pins/etc. Why APM boards are improving, but PX4 is not? 3DR not planning it as a head board for future development? "
"PX4 is cool and seems much more powerful, but I don't understand: what is the official 3DR roadmap for this boards?
APM 2.5/2.6 now looks like the complete solution: it have the case, new compass at 2.6, etc. Improving 2.6 seems strange btw,…"
"I ordered LEA-6H on store.diydrones.com, but cannot launch it in U-center.
Some strange behavior:
- default speed is 38400, usually 9600 on other models
- when I switch output from UBX to NMEA, data flow is stopped. No NMEA data from gps.…"
"BTW, guys, take a look to the my recent flight by route, with W3 set to RTL.
Everything was OK with THROTTLE level, but it was about 400m distance, not 700m. May be algoritm was wrong on a big distances?
"Yes, I really don't understand whats happened.
Look at the graph: after arriving to the first point, copter set throttle lower and go down, altitude error began to grow, but controller does not increase the throttle to compensate it. Why? And…"
"I have take a look at your logfile, but nothing strange was found... Some strange was appear target alt - it was set as 30m for both waypoint, but when copter was starting it was 30,0m and when it's start to travel to WP2 - the target alt was…"
"I had some problems, with my Futaba.
- Original Futaba receiver - works well.
- Orange RX receiver - works well.
- Corona receiver - jitter on 5 channel (F/S was switched off and settings were checked).
So, some hardware may be incompatible,…"
Hi all. I'm glad to be on this forum, maybe my information will be useful.Today I did the mission flight, it was not my first flight, and everything was ok before.I've added 2 points: first at 700meters from start point, type WAYPOINT, second is RTL command. On both points attitude was set at 30meters. There was 3DR on board and voltage sensor, telemetry was writing. ESCs was DJI Opto 30A, external BEC was powered the board.And so, the problem: quad flew success to the first point, rotated and…See More