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  • ok so onto the build,

    here I have the damaged h500 frame from droneshop that crashed,
    it currently has 810kv rc timer motors, spinning a 1245 prop , these motors are designed for 1045 , but for some reason my friend used 1245 and it handled fine,

    as you can see I have the 13 inch carbons going on ,
    the NEW arms that are going on are 33cm long .
    compared to what is currently on in this photo (17cm)

    3702318722?profile=original

    as you can see the new layout is a hell of a lot bigger ,

    3702318843?profile=original

    measures in at 1000 size ,
    or 850 if I trim the arms so the props only JUST fit without overhanging the frame

    I don't want any overhang of the props/frame as I want it to be as efficient as possible.

    oh look! heres the postie... brang me my new DJi E800s from buildYouOwnDrone

    3702318789?profile=original

    http://www.buildyourowndrone.co.uk/d...exacopter.html

    I purchased them separately not as the tune kit as I already have ESCs and I only need 4

    more to follow... feel free to jump in

  • hi guys, been flying and building for a good few years now.
    i was out of the air for 2 years but now im back up and flying again, missed it alot, all of my previous builds were modded versions from bought frames,

    i had a Hj H4 Folding carbon fibre Quadcopter frame from ebay and built ontop of that.
    photo and specs

    3702319014?profile=original

    it was pretty stable.

    after getting bored of the Flight time of ten minutes.. converted it into a very rough built Y6 gaining 15 mins flight time from it.

    3702319033?profile=original

     i sold up my gear after a while due to personal reasons

    in the past 2 months ive now bought back into the hobby luckily buying
    this H500 Folding carbon fibre Quadcopter complete built & test flown system from a friend for a very cheap price.

    3702318940?profile=original

    a fraction of what it retails for from

    http://www.droneshop.biz/multirotors...wn-system.html

    its a stable platform but i think i overloaded it with weight from fpv setup and gimble , it resulted in a crash on my last flight

    https://www.youtube.com/watch?v=DV5Nzlp0RvU



    This altitude play Ended VERY badly (4 min 23 sec)


    whilst out flying the other afternoon , my h500 quad decided to go awal for no apparent reason , it switched itself to LAND , i had minimum stick input for roll pitch yaw, and had zero throttle control. using the telemetry link and mission planner i tried to get it out of LAND mode back to stab but no luck.it ended in a tree with broken arms, props, and landing gear,

    so NOW ONTO THE REBUILD /UPGRADE ! >> more to follow after this post !
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