I built a quad with Xproheli XPX frame. I used all of the recommended parts, motors blades etc. Tiger Motor MN4012 480kv Navigator Series, 14" APC props Naza m V2. I've tried recommended gain settings and experimented with others. The quad wobbles bad on descent and in wind. Way more than any other multirotor I've had. Xpro tells me it's how they are. Doesn't seem right to me. Any ideas or thoughts would be appreciated.

Views: 181

Reply to This

Replies to This Discussion

I think I figured out one of the arms was tweaked out of the box. Flying better.

Reply to Discussion


© 2019   Created by Chris Anderson.   Powered by

Badges  |  Report an Issue  |  Terms of Service