Share 'strange behaviour of pixhawk-request help to understand'
I am building a 1300mm octocopter with 30AH lipo. I want to be using a tegra tx1 for onboard visual processing coming from a sony a6000.
I have built the drone and assembled it. I have configured it as usual. I was using the external compass on the m8n gps. and when the compass calibration happened both of them had similar reading all under 150. I have also done a compass motor calibration f…
You can share this discussion in two ways…
Share this link:
Send it with your computer's email program: Email this