Erik Unger's Discussions (3)

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RPM oscillations on yaw

I am working on a 1.2m Quad with Pixhawk. First I had problems with the green Turnigy Multistar ESC, but after flashing SimonK they work very smooth and sensitive.

Now the problem: When increasing yaw over 50% the two slower rotating motors start to o

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Help, I think I have built a monster...

I tried to create a really powerful quad with HK components and an APM 2.5. It looks like I have created an unflyable monster:

The first flight attempts were a disaster. Upon just touching the throttle it jumped in the air and flipped on its back fast

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