I just built a new AMP 2.8 build. Its my first time with ardupilot. When I do a test flight it seems to behave fine foe 20 seconds or so and then it takes off either left or right and my stick inputs…Continue
"Large compass offset is caused by magnet interference or metal too close to the flight controller.
Check that there is not something magnetized.
Sometimes just using a standard camping compass you can see if the needle moves strangely when placed…"
"That is great info Mike thank you so much! I had a 1300mah Batt on it that I use on a 250 size quad. I have a 5000 for it though. I will also hook up the buzzer and see about turning up the LOG info size.
Any advice about the compass situation.…"
"From the first log the reason you lost control was because the battery failsafe activated which causes the copter to fly home and ignore input from the operator. You must not have a buzzer attached otherwise you would have herd the sound.
"I figured out how to export the logs. I attached two of them.
It flies fine for a few seconds and then disregards my inputs.
I have also been unable to satisfy the compass calibration routine.
My flights have been in stabilize mode. so maybe …"
"We need more information to go on here. What size copter, what radio are you using and what receiver is connected.
Did you check the motor order in Mission Planner, did you calibrate everything. Are you using a GPS.
Do you have a…"
I just built a new AMP 2.8 build. Its my first time with ardupilot. When I do a test flight it seems to behave fine foe 20 seconds or so and then it takes off either left or right and my stick inputs dont seem to have any effect.The flight controller can hear me because I am able to disarm from the transmitter.But i cant throttle down or control the quad normally.As this is my first time with these kind of flight controllers, is there something I should be looking at first?See More