Started this discussion. Last reply by logic Oct 27, 2013.
Hi everyone,I just took my 3DR Hexa (APM2.6, ArduCopter 3.0.1) for its first flight and tried testing throttle failsafe. While hovering about 1m above the ground, I switched off the RC and expected…Continue
Tags: unexpected, climb, rtl, land, failsafe
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