May 13th, first test flight of both the Lego UAV and the stealth "minimum" UAV at Alameda Naval Air Station. Video coming soon.
--Flight stabilization: Worked. a little rocking, but nothing too serious
--Autopilot: Sort of worked. Rudder throw needs to be increased. Heading change induced expected counter force by stabalization, which increased rocking. As a result the turning was very gradual. That needs to be faster
--Video: Ground team forgot to raise the receiver antenna, so signal was weak except when the UAV was overhead.
Ony tested airframe and stabilization. Airframe flew normally. Stabalization induced strong down elevator and aileron deflection, despite multiple calibration attempts. Something either wrong with set up or hardware.