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RT @f1tenth: Say hi to our newest #F1TENTH creation for @ieee_ras_icra next week in Philly. It’s going to be huge! 😎 🔥 @AutowareFdn @PennEn…
Our next Virtual Race will be on June 4th:
https://www.meetup.com/DIYRobocars/events/285787423?utm_medium=referral&utm_campaign=share-btn_savedevents_share_modal&utm_source=link
RT @SmallpixelCar: Noticed my car zigzagged in last run. It turned out to be the grass stuck in the wheel and made the odometry less accura…
RT @SmallpixelCar: Test my car. RTK GPS worked great. Thanks @emlid for their support. https://t.co/EkQ6qmjmWR
RT @chr1sa: @kane That's @diydrones circa 2009. Still have a box of those Canon cameras that we used to strap into planes, just like this.…
RT @chr1sa: Our next @diyrobocars race is going to be outside at a real RC racetrack in Fremont on May 28. Fully autonomous racing, head-to…
RT @f1tenth: Our Spring 2022 F1TENTH course @PennEngineers is coming to an end with a head-to-head race as a big finale. So proud of our st…
RT @DanielChiaJH: I wrote a thing! Throughout the development of my @diyrobocars car I've been using @foxglovedev Studio to visualize and d…
RT @SmallpixelCar: My new car for high speed. Low body, everything ( @NVIDIAEmbedded Jetson Xavier NX, @emlid RTK GPS, IMC) under the deck…
RT @f1tenth: F1TENTH Race training setup @PennEngineers for our upcoming ICRA2022 @ieee_ras_icra competition. @OpenRoboticsOrg @IndyAChalle…
RT @fatcatFABLAB: Proud to be hosting a restarted DIY Robocars NYC Meetup April 26. Come by if you want to talk about and race self-driving…
Replies
Did you find a solution to this problem? I am experiencing a similar issue
Did you ever find a resolution?
Here is what the voltage looks like
Both.
The 3DR module was working correctly in February as shown here:
https://www.youtube.com/watch?v=VQFNICnsTk0
Early this month the pixhawk started giving readings of 14V (alarming because we are using a 3S battery). I used the power module "other" option to re-calibrate at the measured voltage but was seeing similar results when capturing the log as above.
After similar results I bought a power module from wasooo to see if the results would differ but they did not and this module did not produce a log of the current.
The Vcc is fine to the pixhawk under the load as referenced in the wiki:
http://copter.ardupilot.com/wiki/common-diagnosing-problems-using-l...
However, there is no common diagnosis for the "Battery Issues" log and I would like to know if this is typical.
Thanks,
Louis