hi all lets start that i'm newbie to this (but with 15+ years of aerospace electronic design... which makes my situation not that good :)
So ive build quad with ADP2.5, all OK,
problem #1 radio calibration seams to be reset when i unplug the buttery, as result next time battery plugged in i get like 60% trottel when stick is at max ==> cant fly on that power
problem #2 in around 1-3 min of fly props spinning i get board doing to disarmed state and i loose control of motors. Ready LED starts blinking red
I might be doing something wrong so hopefully some experst can point me out to righ direction to make this thing fly before i go nuts and build my own motherboard :)))
Tnx
Replies
Join my club, this retired elec eng/college prof is getting stumped too easily.
I tried to lift off the floor for the first time and the same happened. Lots of noise though. I cant wait unitl I hit 100%. :) Will probably get run outdoors by my wife.
I havent figured out how to reverse the throttle on my Turnigy 9x controller, either.
Bo