hi all lets start that i'm newbie  to this (but with 15+ years of aerospace electronic design... which makes my situation not that good :)

So ive build quad with ADP2.5, all OK,

problem #1 radio calibration seams to be reset when i unplug the buttery, as result next time battery plugged in i get like 60% trottel when stick is at max ==> cant fly on that power

problem #2 in around 1-3 min of fly props spinning i get board doing to disarmed state and i loose control of motors. Ready LED starts blinking red

I might be doing something wrong so hopefully some experst can point me out to righ direction to make this thing fly before i go nuts and build my own motherboard :)))

Tnx

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  • Join my club, this retired elec eng/college prof is getting stumped too easily.

    I tried to lift off the floor for the first time and the same happened. Lots of noise though. I cant wait unitl I hit 100%. :) Will probably get run outdoors by my wife.

    I havent figured out how to reverse  the throttle on my Turnigy 9x controller, either.

    Bo

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