Hi all , Come back again after test,
Hardware :
My Own plane , similar to Skywallker ,
Flight controller : Pixhack CUAV .
GPS : Ublux 7
other additional tools ,
Software :
Firmware : Arduplane 3.4
GCS : Mission Planner.
with out AirSpeed , throttle cruise 60 ,
the plane takeoff good in stab mode then start big pitch up then stabe while trying to control the plane , many time it make a big pitch up ,
change mode to auto , this time the throttle works good but it did a pig pitch up again to stall level then I take control with stab again many time
I don't know what happen this time and what is the reason of that ,
the log file size is 57 MB and try to add to winrar it become 11 MB but limit attach file here is 7 MB
How to Upload it for you
hope I can find answers for my problem
best regards
Replies
thanks
here is the log file for the small first test
2016-01-15 12-03-20.rar
How well does it fly manually? Its always best to take one problem at a time. Be certain that your design is stable when flying manually to reduce the amount of correction needed which will also give you a more stable camera platform. It sounds to me like your horizontal stabilizer is either too small or too close to the center of lift and/or your CG is very far back, very close to or behind the center of pressure.