Today I flew 10 km away and back totally in Auto Mode.
Until 2200 meters to home in return, everything was perfect.
As you see in the video (after 0:42), while nearing home, plane suddenly rolls to right then left then right again and levels, but from
Read more…Hi.
My plane autonomously climbed to 1700 meters on LOITER UNLIMITED mode 400 meters far from me. Then I switched to RTL.
Plane started to descend smoothly and return to me. (It was over me already.)
After starting descend, at one point, nose dived appr
Read more…I turn throttle failsafe ON and adjust threshold to 1050.
Adjust my radio to set throttle pwm to 1000 when switched off.
When I switch off my radio, failsafe kicks in and first it goes to CIRCLE mode then 15-20 seconds later to RTL mode.
But I want APM
Read more…When I fly and return back home, I plug APM2 into my computer and it downloads .tlog files.
But if I press "Load Log" button and select one of the logs, I can not play and see my plane moving on the map properly.. Why?
Does it work only if there is 3dr
Read more…Hi. I've just installed AttoPilot current and voltage sensor on my APM.
On my plane, everything is powered from ONE battery. (Motor, APM, EzUHF Rx, Video TX, minimOSD, FPV camera, servos, .....)
When I plugged in my battery and let the system boot up,
Read more…Hi.
My plane crashed and usb connection port has broken, detached.
I connected boards to my computer like shown below using standard usb cable.
Eveything works fine, uploaded new firmware, calibrate RC inputs, roll, pitch, etc.. Fine...
But GPS (uBlox) i
Read more…Skip to 02:32..
When I switched to RTL, it banked 60 degrees left, full throttle, nose down.. Why?
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Hi.
In wiki, it is said that we have to calibrate rc inputs first, then load a configuration file if there is one for our plane.
When we load configuration file, RC calibration is gone, isn't it?
So should we calibrate RC again after loading PID file?
Th
Read more…Hi.
When setting up APM on the ground, on Flight Data tab of the software, pitch is going up and down continously, if I switch to Stabilized mode, elevator replies to this situation, moves up and down.
This occurs ONLY when the uBlox GPS is connected.
I
Read more…My Skywalker setup was working fine until I changed my Radio and RX.
After change, I reset everything and calibrated radio.
Now,
with airspeed sensor attached and turned on, aircraft pitches down when switched to RTL,
in same position, I disable airspeed
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This is a Skywalker with APM, uBlox GPS and airspeed sensor.
PID parameters are loaded from Skywalker.param file which downloaded from APM Wiki.
What can be wrong?
Please help.
Hakan Karakurt
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