Another crash.. this time thanks to the 3DR power module. I used to have an external UBEC to power my APM and it was actually working pretty well. But 2 weeks ago I decided to get a 3DR power module to make things even better and have a all-in-one pr
Well today I went for a test flight, trying to get my octocopter under control because I have an important demo to do on Saturday for a potential client. It did not go as expected. Here is my config :
Really need your help here. I've been trying to fly my new Octo X8 with the AC3.0.1. Compassmot is at 30% which should be ok. Problem is that the copter spins when taking off all by itself. I had to jump on the ground to avoid collision with the
I've been trying to analyze 2 unexpected RTL mode switch I had in 2 days. I was flying my octocoper with AC3.0.1 on it in stabilize mode. Flying perfectly. Then switched to Loiter, and it was ok. Back to Stabilize then it started to climb alo
I need some help with a Freefly 360 modified servo for the tilt axis that I use with an external pot. I'm using the Rusty's gimbal with the 5k external pot (PEC pot) on the tilt axis. From the servo, I got 2x3 wires coming out. One of the wir