Hello,
I am having some problems setting up my 3-axis Allsteady-5 gimbal from Turbo Ace for RC pitch control. I am using the Simple BGC GUI version 2.41b5 (recommended by Turbo Ace) to adjust any settings for the gimbal. I have the Futaba T14SG transmitter set up on the DJI's A2 flight controller. Everything is working fine on the multirotor end.
The problem I am having with the gimbal is that it only responds properly to the multi-rotor's pitches when I don't have the RC pitch control selected. As soon as I "write" to the gimbal that I want RC pitch control it starts responding incorrectly. A video is worth a thousand words, so here is what I mean: https://www.youtube.com/watch?v=OnCvFDpvdAo&feature=youtu.be
This is way beyond my gimbal tinkering experience, so if anyone recognizes what is going on, I would greatly appreciate your advice. Clearly it has something to do with the RC signal input, but since this particular hexa and the gimbal are sold with the exact same Futaba radio that I've got on it, and the same A2 flight controller, it's got to work somehow.
Thanks,
Jan
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