Hi all,
I'm attaching my log from our last flight as our little quad went completly bonkers before it crashed.
Short after takeoff it went completly out of control, no response at all from RC or Telemetry and then crashed near a pond (thank god).
But the mistery was about to begin when we started reviewing the log and found out that the trigger was the failsafe error Err: EKF_CHECK-2 / Err: FAILSAFE_ EKF-1.
In understand these two were recently added to APM, but this ain't the first time I see this sort of thing happening.
I'm attaching my log in hopes for some guidance.
Thank you all!
Replies
Not sure how you attached the bin..
here is a link to mine in drop box
https://www.dropbox.com/s/631xegi2gfq6b99/2015-04-06%2013-46-59.bin...
Later on in the log it looks like bad vibrations, but the initial error looks like the OP - huge requested Yaw triggering an EKF fail error. Your ErrYaw is also huge all the way along, so you should look at the vibrations anyway.
what is a OP
Opening Post
Found out how to Attach file.. here are a few logs from when the error was occurring..
2015-04-11 15-35-56.bin
2015-03-10 14-19-42.bin
2015-04-06 13-46-59.bin
You have bad vibrations. You should fix those - it is the cause of most of your problems.
Bad Vibration.. What are you looking at so I can see what you mean? and besides balancing props how do you get rid of that?
Sorry I'm a newb!
http://copter.ardupilot.com/wiki/ac_measuringvibration/
ya I read all that.. still don't know how to fix it
Balance your props should improve that greatly