APM Newb Flight Issues

Hi All,So I am moving from a KK controller to a APM 2.6 with the Ublox Neo 6M gps.SunnySky 980kV motors3 multistar opto escs and 1 non opto powering the controller.3s lipoFlySky T6B Radio - Mode 2I have gone through all the necessary steps to get my Spider style quad in the air. So my issue is the quad is very unstable in the air. I bring it up about 5 feet and if i move the roll or pitch at all it gets pretty hairy like it can't stabilize when i let the sticks go.Here is the log from my last flight. After a bit of searching i found i needed to reverse my aileron which shouldn't affect my stability issue. Let me know if anyone sees any glaring issues. I have not tried adjusting PIDs just yet as i though it would at least somewhat stable with the base config.Any help is appreciated.

IMG_2777.JPG

2014-10-21 05-22-10.log

LogAnalysis.txt

You need to be a member of diydrones to add comments!

Join diydrones

Email me when people reply –

Replies

  • Thanks for reply. I have it fairly stable now. Surround would never complete so I took the pic values from the iris and it got me close. I also minted the Apm on gel tape and that helped as well.
  • Forgot to mention APC Multirotor 10X4.5 props.
This reply was deleted.

Activity

Neville Rodrigues liked Neville Rodrigues's profile
Jun 30
Santiago Perez liked Santiago Perez's profile
Jun 21
More…