Hello!
I had an issue coming out of loiter mode, which saw a lot of destruction to my quadcopter, but it has been repaired. I'm still fairly new to this so I am hoping for a little help.
Here is a video of the behavior:
And here is what I see in Mission Planner with the Quad resting on a level desk:
Any help would be greatly appreciated. The motors all seem to be fine, and the ESCs were calibrated along with the Radio.
Replies
Hi Don,
Firstly, look at the direction of your motors, some of them seam to be spinning the wrong way round.
Secondly, you need to re-level the copter in Mission Planner.
That should get you going.