I've just loaded the new Arducopter 2.7.3 in my Octocopter and now it doesn't give the motors enough throttle to lift off the ground . It was flying fine before ; I've calibrated the ESC's again and no difference .What's going wrong ?
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Hello,
With the new firmware versions, the motor control was reduced (
This produces a big loss of power!
You can look at the graph below:
Red = input receiver
6 = other color out motors
How to regain power???
Capture.JPG
Have you gone through the regular setup, including RC calibration? If so, maybe try CLI setup/erase /reset to clean your EEPROM settings and try again.