Hi,
Working on my 1st build from scratch (Tarot 650 Sport) with Pixhawk running latest Arducopter. Esc's are hobbwing x rotor.
Ive fired her up for the 1st time & it appears that one motor is very slow to respond & at low throttle doesn't spin at all.
Also noticed that motors give off a beeping send when powering up yet after arming this beep goes away.
Hoping for ideas on what data I can pull from the telemetry logs to help work out whats going on.
Thanks in advance
Replies
Turns out one of the esc's wasn't synced. Found this video very helpful https://www.youtube.com/watch?v=Hl-Q7RPOn18