Hi,
As you can see in this video :
When I slowly raise the throttle, it tends to go back. If I raise again, it fall.
What can be the problem. I see two possible problems :
- On the radio calibration, Yaw is at 1474 when there is no input.
- Ths esc calibration was not did exactly like this : http://copter.ardupilot.com/wiki/initial-setup/esc-motor/. It did not the 4 bip for 4S battery. It did two bip and a long bip when the throttle was high and a long bip when it was low.
I bought this kit : https://store.3drobotics.com/products/diy-quad-kit
Do you have a solution?
Replies
I redid the ESC calibration and it do the same thing than in the doc but I have the same problem.