Hi, I need help my log file. I made fy680 convert to x8. I have orijinal pixhawk, 10000mah 6s, Atto pilot 180a, 5v bec secondry power for pixhawk, dragonlink rx... I had naza but I sold it. I bought pixhawk and I first fly yesterday. Thanks...
You need to be a member of diydrones to add comments!
Replies
I want to add new question. My octo will be 5-6KG auw. Which I will use PID tuning. Stoke or custom. The other question, I dont understand that balance/twist = NA, PM = NA and Pitch / Roll =NA on LOG ANALYZER.. I first tryed takeoff my frame fliping to left. Than I could takeoff. You can see my video. Is it okey.?? Thanks again..
Thanks for reply, sorry for my bad englsih. I did first flying. I am very happy. I dont understand that balance/twist = NA, PM = NA and Pitch / Roll =NA in LOG ANALYZ.. I first tryed takeoff my frame fliping to left. Than I could takeoff. You can see my video. Is it okey.?? Thanks again..
Everything looks good in the log. May need some Pitch/Roll tuning but it is a large copter. At the end of the flight though the radio/receiver lost contact and you had a failsafe set and it when into RTL and landed itself where it took off from.
Hi again. I add takeoff video and detail lof files. What is the problem. Tahnks again..
FIRST FLY TAKEOFF TRYING.mp4
TAKEOFF.mp4
2016-10-15 12-10-15.rar