Replies

  • Did you manage to fix this problem? I am having a similar issue. When the board is stationary on the bench (no GPS lock) the roll /pitch sensor output is stable. As soon as GPS gets a lock the pitch/roll sensor output becomes unstable and does not settle down to a steady value.

This reply was deleted.

Activity

Neville Rodrigues liked Neville Rodrigues's profile
Jun 30
Santiago Perez liked Santiago Perez's profile
Jun 21
More…