Pinar Cokum's Discussions (2)

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Loiter test and crash with 2.0.32

Yesterday I tried the code 2.0.32 for the first time in the field. The first flight stable mode worked very well.The second flight, I tried to Loiter mode. The first experiment is very good.But the third and fourth flights, when I switch loiter from

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Downgrade with APM Planner

Thank you for APM Planner. This is nice job.I had some problems ArduCopter version 2.0.26. At that moment I wanted to return to the old version. But i dont want to use Arduino IDE.Some people may want to downgrade to the desired firmware easily. Is i

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