First flight went well. Was able to test Manual (Works! :D), Stabilize and RTL modes.
The plane is a semi-stock Parkzone T-28 Trojan. The servos are all stock. ESC and Motor are upgraded to E-Flite 80AMP ESC and Power15 Motor. Generic 5v BEC powers APM and Radio equipment and nav lights. RC Radio gear is JR 2.4Ghz. Telemetry provided by 3d Robotics Telemetry Radio.
This was using older firmware (Stock as of when the board was hand made by the awesome folks at 3dRobotics, not updated to new MAV1.0 FW). I have recently updated to current firmware (Using Mav1.0), and I am in the process of testing all settings and preparing for my second flight. I would like to add a Amp/volt meter, and AirSpeed sensor before my next flight, as more data = good thing..
Comments
Nice flight. I would like to pics of your plane on your diy page as my first APM flight was with a PZ T-28.