"My /etc/config.txt file:
# Generic Quadcopter xset VEHICLE_TYPE mcset MIXER FMU_quad_x# PX4IO PWM output will be used by default
set PWM_OUTPUTS 1234 # Change parameters for the first 4 outputsset PWM_RATE 400 # Set PWM rate to 400 Hz for better…"
"No sorry, you don't need the rc.txt anymore, the autoconfig will do most of that for you. Just config.txt will be fine.
I don't have the PX4 with me ATM, will upload my config.txt later."
"Found out what was the problem, for someone who might experiencing the same issue, it was because the airframe model was selected wrong, and the /etc/rc.txt, /etc/config.txt files not created on the SD card."
Hi Guys,I am using the PX4 FMU V1.7.2 with IO V1.3.1, QGC 2.0.3beta, the latest QGC firmware, Quad with 4 x 40A SimonK firmware ESCs and 2815-470KV motors.The installation/setup was straight forward, the firmware was updated smoothly, the RC and…