2.0.38 Loiter problem crash PLEASE ANY HINT

Hello

I went to a park, waited for gps lock, I was in stabilize 5mts from ground, and switched to loiter, my (all stock) quad did loiter for 20 seconds fine, then "suddenly went very fast in one direction like crazy!!!", I then switched as fast as I could to stabilize, but crashed, even at zero throtle on the floor  it did not stop the engines ... i disarmed with throtle 0 and to the left

 

ESC where calibrated properly, 100% sure no motor/ESC/prop fault, gps locked, all stock 28mm frame, violet motors, 10'45, sonar no,100% lipo charged, magnet yes, it was flying always fine...

 

Notes: when I tried to see the logs, I ve seen only one log 4,6mb!! where I should have been many different files...I do not know why... and when downloading it, stopped saying lat  should be between -180 and 180...and break log download, so cannot post the last flight log :(...

 

what was suddenly wrong????

 

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  • Developer
    Can you access the CLI from Arduino? You can get the logs from there. That would help.
    The engines in that version wind down over about a 3 second period. That's actually removed from the current version, but really wouldn't affect your crash.
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