Hello everyone, I've been working with a new-brand CC3D with Open Pilot. Actually, I've followed the steps shown in the official page of Open Pilot, I've calibrated ESCs, RC, and so on. Here are the setups and a video about the problem. I've checked all and the motors turn in the right directions and so are the propellers.
Hardware setup:
Frame: Quadrocopter Spider X500 TBS DJI
Motors: MultiStar 2212 - 920Kv
ESCs: SimonK 30A
Flight Control Board: CC3D Open Pilot
Battery: LiPo 3S 4200mAh
Propellers: Self-tightening 9443 (Included with the motors)
RC: Turnigy 9X
Open Pilot setup:
Controller type: OpenPilot CopterControl 3D
Vehicle type: Multirotor
Vehicle sub type: Quadcopter X
Input type: PWM (One cable per channel)
Speed Controller (ESC) type: Rapid ESC (490 Hz) Is it correct for SimonK ?
Initial Tuning: Current Tuning
All the other configurations/parameters are the default ones.
With respect to the ESCs calibration, I did it as shown by the setup of Open Pilot.
Should I need to set extra parameters to get it work ? Any ideas about what could be the problem ?
Videos:
https://www.youtube.com/watch?v=jDvVmWZd9o0
https://www.youtube.com/watch?v=O6XL_q9OSzo
Thanks in advance. Any help would come really handy.
Greets.
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