I have changed from a kk2 board to the ardupilot with the latest firmware done al the calibrations but do not have enough power to get off the ground The quad had plenty of power when using the kk2 board . checked the settings in stranded parameters and maximum throttle is set to 1000 .
yet I still have lack of power to get off ground?
Now I am stuck, two weeks trying to get it to work ,might put the kk2 back in at least I can have a fly then???
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In the radio calibration page throttle goes from 992 at low to 2018 at full throttle