Problem with AC3.3 RC5 px4flow

Hello,

I just setup px4flow with AC3.3 today. But When I start takeoff of loiter mode.

But it starts to accelerate away or there is erratic pitch or roll movement.

May I have question to understand what's wrong with my QuadCopter ?

Quadcopter is QAV250, and attachment is log file.

Thank you

2015-06-12 23-45-52 3.bin.rar

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Replies

  • I think the code is probably buged. We have encountered the same problem and couldn't fix it yet and sort of gave up.
    So far we're trying Pixhawk's original firmware.

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