Hello,
I just setup px4flow with AC3.3 today. But When I start takeoff of loiter mode.
But it starts to accelerate away or there is erratic pitch or roll movement.
May I have question to understand what's wrong with my QuadCopter ?
Quadcopter is QAV250, and attachment is log file.
Thank you
Replies
I think the code is probably buged. We have encountered the same problem and couldn't fix it yet and sort of gave up.
So far we're trying Pixhawk's original firmware.