quadcopter yaw at full throttle after simonk flash

I just flashed my ESCs with sinonk.  Since then when applying generous throttle the quad does not maintain heading and there is significant yaw.  Prior to flashing there was no yaw at full throttle.  Is this typical?  What changes to PID would address this?  Thank you!

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Replies

  • Did you recalibrate the escs?
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