I recently revised my miniquad design and have some hardware left over from my first version.
1. Miniquad frame: This frame is built using 1mm carbon plate and 4mm pultruded carbon tubing. Tubing is reinforced with internal fiberglass ferrules that
I recently had a bad crash and the 3.3V voltage regulator on the Oilpan that is located close to the I2C port was damaged. I replaced it with an absolutely identical chip (got the correct part number from the DIYDrones store). Now I have a couple
I suffered a pretty bad crash last week and since then I can't get my compass to work anymore. However, I am not sure if it's the compass that's actually broken or maybe my IMU board.
The compass just outputs 357 degrees all the time.
I'm just starting out with my Arducopter project and still have a lot to learn about the code, so pardon me if this question has been addressed before.
I understand that the autopilot main loop runs at 100 or 200 Hz, I read this in another topic. M