I was flying a new quadcopter on Friday to test the Auto flight mode. I had a successful first mission and I tried to replicate it. Since my last waypoint was facing the opposite direction from takeoff and the RTL kept this heading, I manually rot
I've been flying with my large quad for almost a year, and I've never had an issue with the motors, until a couple of days ago. The quad was flying in auto mode in an area where I have already tried a few times, and it was behaving correctly. Then