After 10 minutes flight my quad copter disarmed and crashed like a rock, and mission planner can not read logged file for this mission can any body help me..
Hithe quad copter fall down with high speed perpendicularly on pix-hawk autopilot controller, and when i revised the log i saw that the throttle (RCOUT) increased to maximum on channel number 2 as you see in figure attached and bin file, please can…