"1) Don't hesitate, safety will suffer.
2) Buy a genuine component will cost you 100$ but will inmediately work.
Buy a clone component will cost you 30$ but will take several days to get it working.
3) Your copter will crash, no matter how good…"
I tried changing the value to 500cm/s in standard parameters, but it would always change back to the faulty 327637cm/s.
Only when I changed it in full parameters list it did finally keep the value of 500cm/s
"My copter is fully functional now, there were too many wires translating vibrations to my apm via the connections. I loosend up the wires so my apm could move completely free.
Johann considering your problem with the drifting to the right, I…"
I will try rearrange my wiring around the apm to minimize the vibrations and look at my logs for x/y/z vibrations in a coule of hours.
Will post the results and my findings ASAP.
Hello fellow pilots,A couple days ago I was flying my quadcopter running on apm 2.6, wich was working fine.Stab, Althold, Loiter and Auto mode worked flawlessly.Until yesterday, when I switched my flightmode to Althold or Loiter, my copter…