Hay Guys... I am using Pixhawk with 3.3.3 quad. We use factory PID values. The first flight was in POS HOLD mode at an altitude of 7 meters. There was a slight wobble and jerk in the quad. We flew for about 4 mins. The next flight was the same POSHOL
I was flying a 450quad with pixhawk3.3.3with vibration dampers, M8n gps, 3DR telemetry, BEC module and futaba transmitter. I had a clean fight in stabilize mode for about 3mins and then quad suddenly yawed in counter clock
I am using a pixhawk3.3.3 with a quad. yesterday I was flying in altitude hold mode, suddenly quad flipped and drown into a pond. I couldnt recover pixhawk, esc and battery. out of four motors two were good and we couldnt check other two. ther
I calibrated the bec module in initial setup, set measured voltage 12.3 after measuring the battery volt by a multimeter. after a flight, I found that the voltage does not change in the telemetry data and In dataflash lo