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Activity Feed

moriarty replied to Juan's discussion Iniciando mi uav
"Hi Juan. This looks intersting. why not use px4 platform instead. Are you developing this for long endurance ."
Nov 28, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"Hi Greg,
thank you for the insights. I am using a 30AH,25c TATTU battery with foxtech S5010 288kv motors with 17"*5.5" propellers.
Also do you think the magnetic field is in check now? and what is this about motor balance .I was not able to get…"
Jan 23, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
" Thanks Javier,
I shall do a flight test with stabilize mode see how that performs Javier Cerna said:
To be completely honest, I'm not sure why that's happening. But try to flight the drone first in Stabilize Mode. In one of your logs, it seems…"
Jan 22, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"Hi Javier,
Thanks for the Suggestion. I shall check on the Battery and the Motors. But how do you explain the volatility in the voltage and the magnetic field. some flights show good voltage some show a bad difference and same is the case with eh…"
Jan 22, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"HI all
today I performed my flight after much suggested changes in the power module and other power issues.

FIRST FLIGHT:
Test: Autotune = UNKNOWN - No ATUN log dataTest: Brownout = GOOD - Test: Compass = FAIL - Large change in mag_field (59.65%)…"
Jan 22, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"Hi Greg,

Finally I had my attopilot 180amp current sensor delivered. I have bench tested the drone before taking it to field for an actual flight. I also did an auto analyse on the flight log. interference and other parameters seem to be in check.…"
Jan 20, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"Thanks Javier for the suggestion. I found an interesting 180 amp attopilot current sensor on sparkfun and got that instead.  Javier Cerna said:
Regarding the power module, you could use this one, from 3DR:…"
Jan 19, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"Hi Greg,
thank you so much for the support through out. I apologise for the late reply. I have recently changed my autopilot, Compass, shifted the battery a little further down and moved the autopilot also a little above its previous position. I…"
Jan 19, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"my AWP now is about 9 Kilograms Luc Maximilien said:
1200 watts to hover , wow !
What is your AUW ?"
Jan 7, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in PIXHAWK
"Hi Greg
thank you so much for the support. I have actually tested the drone yesterday again. I have moved the compass away from the battery, I have put the battery below the drone and the compass on a mast. and yet it had the same result although I…"
Jan 7, 2018
moriarty replied to moriarty's discussion strange behaviour of pixhawk-request help to understand in ArduCopter User Group
"I did the compass calibration on a home site and did not perform onsite compass calibration Paul Tegler said:
did you run the compass cal at the flight site, pre-flight???
....or did you rely on a 'home' cal before traveling to the site...
ptegler"
Jan 5, 2018
moriarty posted a discussion in PIXHAWK
HiI am building a 1300mm octocopter with 30AH lipo. I want to be using a tegra tx1 for onboard visual processing coming from a sony a6000. I have built the drone and assembled it. I have configured it as usual. I was using the external compass on…
Jan 5, 2018
moriarty posted a discussion in ArduCopter User Group
HiI am building a 1300mm octocopter with 30AH lipo. I want to be using a tegra tx1 for onboard visual processing coming from a sony a6000. I have built the drone and assembled it. I have configured it as usual. I was using the external compass on…
Jan 5, 2018
moriarty posted a discussion
HiI am building a 1300mm octocopter with 30AH lipo. I want to be using a tegra tx1 for onboard visual processing coming from a sony a6000. I have built the drone and assembled it. I have configured it as usual. I was using the external compass on…
Jan 5, 2018