Pixhawk - ArduCopterV3.2.1 - quad copter - Futaba R7008SB

Today I updated Mission Planner to 1.3.29 build 1.1.5646.37690. After the update I went through some settings and found that throttle became yaw and vice versa. I didn't change any setting in my Radio nor Pixhawk. I have no idea why this changed. Did anyone else see this issue as well? What is the purpose of changing this?

Any advice will be appreciated.


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  • I had that happen also. There is a newer update that corrects it. 1.3.30.

  • Same thing happening to mine.. I hope someone will help us outta here!

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