Discussion group for ArduCopter users
Drone flying to non visible point
Hi there,I encountered a problem, while flying in auto mode, with approching to point that was not set by trajectory and is not visible after downloading mission from flight controller by Mission Planner. Does anybody encountered similar problem. The situation is that in the middle flight I stopped the UAV and uploaded new mission and after changing to auto mode it starts to fly in some direction. It goes straight to some point, so I assume it's not mechanical problem. I attached the link to…
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This is the same set up as I have and the 11x4.7 fit fine on mine. You may want to reach out to 3dr or udrones and ask them what is up. It would be nice if they provided some type of guide for the set up even when they are RTF but i guess thank goodness for the community.
p props in correct location now.. clearance still an issue
Andrew. Looks like you have a big problem. I am not sure if 3DR frames are designed for big motors and big propellers but way how they are in your hexa is bad and you cannot use it like that. all jDrones frames are fully tested with 12" propellers. I would suggest to use only 10" props on that your current hexa.
Hello.. Shiny new hexa with all the toys about to leave bench (I hope).. however prop clearance issue! Or am I missing something.. 880 motors 11x4.7 props
thanks
2012-12-09%2020-01-10.tlog
Hi Guys
I was in the middle of tuning for my Loiter and suddenly the quad started coming down out of control and crashed. Luckily no damage but it went out of control. this is the log i appreciate if any one can help and see what went wrong. thanks
2012-12-09%2020-01-10.tlog
OK I got the Loiter going almost good. I had problem with my CH_6 knob on TX. fed the info directly from the ground station. all good for now. Thanks.
@Randy
Randy thank you for the response. Frankly I dont really know what to look for in the log. any idea what i should expect in the log? sorry I have never done this before.
@Avionics
Have you reviewed the logs? That would be a good starting point to see what is happening.
Randy