Hi,as you can see in the video, the copter keep oscillating strangely. At first, I thought it was just because rate_p has been tuning too high. Then I lower all of the PID parameters but problem is still there. I've been trying to set only one…
"I was following your tips step by step, but there is two major problems:
1. successfully setting rate_P to 0.10 and rate_D to 0.006, however, when next day I tried to go on setting rate_I and the copter started to oscillate seriously, and…"
Hi, since my 3DR radio was broken, i'm know trying to connect MP via blue tooth device(HC-06).however, after 3 sec from pressing "connect" button, it always show that "connect fail" (LED on HC06 still blinking )and today I saw someone solved this…