I setup again my arducopter after been away for a long time. I must say that there is a big difference in stability but i don't seem to get loiter tuned in. I have the "toilet bowl" effect around the hold position and i don't know what settings i
I have one of the first imu type the foxtrap one. I tried to found the solder pads to fix the drifting issue as described in the wiki but the board is different. Is there any thing i can do or leave it like that?
Hi.I am looking information on the quad V frame setup. I see in setup that there is as an option but could not find any info on this. Also are they any plans for Y4 setup (like a tri but the "tail" has 2 motors counter rotating)Thanks
Hi, i have installed my magneto to the oilpan and load apm compass test. i have all 0 on the serial. I have check all soldering, and the soldering blob is correct. Also i have 4.7V on vcc. Any ideas on fearther troubleshouting? Is the magneto faulty or