So... I've got one of the original APM2 board, decent ESCs, motors, props, etc... I basically have a totally working ArduCopter from years ago, but never flew it much because of how difficult it was to keep in the air and how much trouble I had filmi
So I've been tracking down some motor/ESC related problems and today I replaced a bad ESC from a motor that had been "stuttering" then giving up as it got too hot. The new ESC is in and working and the motor does start up now....
So..... I guess you could consider me a bit of a nerd gone corporate sell out. I'm all for open source, home grown, new idea, etc..... but in the business world, it almost always means a loss of high availability and redundancy. So my brain is just w
When I first start the quad it seems like everything is fine. (maybe because its all cool?) Then I can fly around for a few minutes..... seems to stay in the air with no problems, fairly level, ALT_HOLD works (ba