Hi everyone, I thought it might be interesting to post what it just happened to me last Friday. I was flying my Octa-Quad with AC 3.4.dev (an old version that I use for testing, but the very same happened with the most recent 3.4.6 when I tried in an
Hi guys, in these days I've been flying with a beta version 3.4-dev (9a09a86b). The reason why I'm using it instead the released 3.3.3 is because I found it more "stable". As soon as I upgraded to 3.3.3 the position controls happened to be very nervo
Hi guys, I have not followed the last release, so I got very upset when I updated my old, steady 3.2.1 Octa-Quad multirotor with the new 3.3.2. Of course I do realize that my system is kind of a mess, because I am using that multirotor for research a
I have just bought a PX4 Flow module with sonar sensor and connected to my Pixhawk board using the i2c cable. I've followed the instructions in this wiki page.
Actually I can't see any data from the OF, neither in the telemetry nor in the log