"also after further investigation in raw data looks motor 1 ,7 and 8 be asynchronous in stabilize motor and with no move on frame please see video here"
24 log it was the first crash 39 was the last crash as i mentioned the setup is the same only difference was the flight control due to old one it was defected in IMU so according answer…"
"both is crashes with same setup difference between them 8 days and a new flight controller the big difference is in 24 log quad flies for one min smooth and problems start when i change flight mode and in last one i just try to fly to…"
"also from previous log without change everything and with crash again look my throttle in and out i attach the log also i think is very strange with the same setup have so big difference propably esc not work correct ???"
"randy i actually take off in 50% and at 1540 in throttle range in pixhawk this is very strange you think maybe esc are not calibrated correct in sbus configuration?
I made now stand alone calibration to be sure everything is calibrated correct "
Hello to all I build a big X8 and i suspect some think happen with my rc mapping when octo starts it feels unresponce with big corrections and hard landings result and some flips whatever i do in P doesn’t affect the system so my next…