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Hello Everyone,
I am having trouble with my copter a few days ago, when I tried to test the failsafe feature of the copter.
I am using 4S 5200mah batter for my copter and my failsafe setting is battery voltage at 14V and RTL should be triggered when it
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Hello everyone !
After I see RTL mode is working quite well from my last flight, I decided to try automode with some
waypoints.
I flew my plane twice with two batteries . My first flight, started by FBWA to take off, change to RTL to check it one more
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Hello everyone !
I am new to pixhawk and ardupilot and currently have some problems with my first flight.
I tested my first built Skywalker 1880mm T tail shape frame and for some reasons, I was not able to get any throttle for the RTL mode Auto mod
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