Paul i did download the 3dr config tool and i made a local firmware update but that dident help
At the past i have change the value TELEMETRY_DEALY from 0 tgat was in stock to 10 and everything worked very good
For no reason…"
About the modes you mention i dont know what happend . i have 2 switches for change the flight modes
1 switch 3 pos is 1 stabilize 2alt hold 3pos hold and when i make the 2nd switch down, the 1st 3pos switch…"
I had a crash with my hexacopter with pixhawk 3.3.2 firmwareI had a perfect flight until i loose my front left prop as you can see at the video. After the prop break from the hub the copter still hold it possition and stabilityI dident understand…