I changed both GPS-Modules to 5Hz, but in loitermode it´s going crazy, the copter is hopping and everytime correcting with pitch and roll.
RTL-Mode = no reaction.
"Hi Randy,
i did not use the buzzer, but don´t ask why..., and i thought red flashing Pixhawk LED is normal when it catches the gps signal.
Should the LED have a solid red light?
I will check the GPS update rate. I never changed the rate. My copter…"
"Hello everybody...
Yesterday i had a new crash with my Hexacopter.
Last month i used v3.1.5, now i´m using 3.2 rc.14 for a few days.
Everthing was great, but my copter had a bad crash, when i activated the RTL Mode and it lands into the highest tree…"
"Thanks, i understand it.
My Pixhawk was connected with 5v from the 3DR Currentsensor and second with an external 5v BEC.
And i cant understand why it should lost the power, when i swiched to RTL Mode....?
Do you mean it was purely coincidence?"
"I was wondering, because all ESCs was beeping after the crash.
Are you shure?
What do you mean with "redundancy?
I checked all wires at first and cant see any difference before the flight :("
"Yes, i meant in balance.
Did you checked vibrationslog?
I had the same problems on my 250mm quad and it was not possible to set vibrations down.
End of project was i sold this quad and built a new one with other motors."
"I had the same problem a few days ago and cant find an answere :(
Mine jumped into failsafe, after lost connection to groundstation, going to RTL and flown over my head into the trees.
I had a lot of luck and it flow height enough, because there…"